UPDATE 15/3/2021
So, after the last round the inlet stub was remounted as described, but without adding the seat for an 'O' ring and allowed to cure.
Re-checked the ignition timing at 0.5°ATDC, as per Tassie Graeme's suggestion.
Again started up no problem with the following settings:
Main jet: 240
Needle jet: 106
Needle: 2A1 with the clip in the 3rd groove from the top (middle)
Slide: 3 anodised slide
Pilot jet: 25
Air screw: 11/2 turns out, off the seat
Cold start jet: 35
Still had the same problem getting the engine to return to a tickover and once warmed through. Again checked for inlet tract leaks, with no result. Replaced the plug with the Gunson to view the flame colour. This remained a light blue inspite of screwing the air screw in to only half a turn from seating. So, time for an increase in pilot jet size. Replaced the 25 pilot jet with a 35 jet that had provided good colour previously (notes!

) and also returned to a 3.5 anodised slide, as from 1/4 throttle on the flame was yellow, with yellow blobs of burning fuel. With this revised set up I was able to attain a good steady tickover at 1,000 - 1,200rpm and a clean increase in revs, without spitting back or blowing the carb off!

Again replaced the plug with the Gunson and could achieve a yellow flame at tickover and then tune this out, with the air screw at ~13/8 turns out from seated. The transition to the slide was more a green than yellow colour flame, with some yellow blobs and at half throttle became more yellow, so it would appear that the needle could be droppeded by at least a notch to the clip in 2nd groove from the top. But, the reluctance to tickover problem remained.
Today, went for some shopping and got lost. After 6 miles, stopped to put some fuel in and the revs sat at 4,000rpm. After putting a splash in the tank, restarted, required a single prime on the cold start and then started on the next attempt, will not start on first kick inspite of being hot! After approx another 10 miles shutting the throttle had no immediate effect unless the revs were reduced by going down the box and using the brakes. Been here before!

This behaviour was consistent all the way home for 15 miles.
Rang AMAL! A technician who appeared to know his stuff probed long and hard about the settings, sucked hard when I said I was up to a 35 pilot jet and finally suggested that I should try specifically pushing the slide horizontally, rather than down and see what difference if any this made. there was also a suggestion, after I confirmed that I had leak tested the whole inlet tract from carb to cylinder head flange that maybe I had a leaking valve guide or poorly seating valve. This thought has crossed my mind as the sustained revs only start once the motor has warmed up.
So, had a mug of tea and a 2 mile walk to ponder. Went and started the engine, single prime with the cold start and then away on the next kick with the cold start 'OFF'. Warmed everything up and when the revs wouldn't die, pushed the slide horizontally to ensure a seal between the slide and body, sure enough the revs dropped back to a steady tickover at 1,000 - 1,200rpm. This was/is consistently repeatable. Bear in mind that this trick is only supposed to work on well worn slide/body combinations and this slide/body combination has less than 10 hours running behind it from new!
I also took my knackered MKII No.3 brass/chrome slide, a MKII No.3 anodised alloy slide, a MKI No.3.5 anodised alloy slide and an old worn MKI No.3.5 'pot metal' slide and weighed them individually on a plastic letter scale that I have. Not to Nigel's standard, but good enough for bush/forestry engineering!

The weights were:
MKII No.3 brass/chrome slide = 75grammes
MKII No.3 anodised alloy slide = 50grammes
MKI No.3.5 anodised alloy slide = 60grammes
MKI No.3.5 'pot metal' slide = 85grammes
This would indicate that the lighter, "less wear prone slides", are in fact more susceptable to fluttering in the breeze in the carb body when faced with the intake pulse forces generated by a lusty single. Hence the use of weighted/heavier slides and "stronger" slide return springs to try and retain control of the slide.
AMAL have back in stock MKII brass/chrome slides, but will they be heavy enough, say 100grammes?
AMAL do not make a "stronger" slide return spring, so what are the alternatives that others may use?
Or should I be lifting the head as well to inspect the valve guide and inlet valve areas, for minute cracks etc that might open up as engine components expand with the increase in temperature?
I am inclined to the former two first.
Thank you for your time and good health, Bill