UPDATE 18/09/20 23:20pm
Aye George, thank you for the additional 'to eliminate' list.
The condenser has been swapped for the new one from the motor factor and mounted in the same position on the coil as the previous one was. That mod was made in 1976 when the original electronic ignition failed and was replaced with Ford Escort points, back plate and a ground down cam with a single lobe.
I have an earth from the engine directly to the alloy plate on which the Boyer box and the Electrex rectifier are mounted beneath the seat and this is also earthed to the frame. There is also an earth wire run from the headlight, back to the coil bracket and then back along the frame spine to the alloy plate earth. The ignition switch is a new key switch from Vehicle Wiring Products and this has a rubber boot fitted to protect all of the connections. All connections are crimped and soldered before either being sheathed by the moulded sleeve and or heat shrink tubing. I haven't tried the disconnect of the Boyer box, but don't think that is giving me problems.
Having just come in from the workshop this is the update on what I have done today. Started the engine that took the usual multiple kicks and spit backs through the carb, after flooding the carb and managed to warm the engine through on a steady throttle at 2,000rpm. Adjusted the carb and achieved a steady fast tickover ~1,500rpm, but then it went walkabout again! Turned the engine off. I have only ever used the short trumpet on the carb as there is insufficient room to fit the race trumpet with the flexibkle mounting. If I mounted the carb to the head studs, then I think I could fit one, but have never tried. The reinforcing gussets bracing the spine tube of the frame to the down tubes onto the rear engine plates get in the way. Main jet in the carb was a 220. Nigel Lacey in perscomms agreed with 220 - 240 main jet as a suitable starting point. I have never had a choke slide fitted to any (2 to date) of my MKI 932 fitted to this engine. A good tickle was always sufficient.
Took the 'SuperTrap' short megga off the shelf and fitted it, with 16 diffuser discs, as it had last been used 20 odd years ago. Tickled the carb, swung the engine over and away it went. A regular tickover at ~1,000rpm was achieved, with the air screw 1 turn out from seated and the slide screw lifting the slide by 1/2 a turn. Taking the motor to 3,000rpm and then letting the revs drop, the tickover became variable but not as excessively as before and would still spit back and die. So it would appear that there is a weak running problem and the unrestricted Goldie exhaust excaserbates this. I also again felt for fore and aft movement in the carb slide and didn't think it excessive, but noticed lateral movement which, I thought, excessive and hadn't tested for before.
Tonight, I went through a box of Amal MKI 932 bodies and bits from a friend who has Norton Commandos and has replaced the Amals with single Mikunis on a twin manifold (Take the hint!

) Amongst this lot there was an apparently unworn body, with no warping to the stud face and when the new anodised 31/2 cutaway slide was tested in this body there was no fore and aft or lateral movement. So decided to use this ex Commando body to replace my current body.
Transferred the air screw, slide screw, complete float bowl and it's contents, changed the main jet to a 230, along with the slide etc. to the Commando body. Then dismantled the stub mount from the front of the carb to use on the Commando body. The new Amal OEM 'O' ring sealing the face would not remain in the machine groove in the face of the carb flange and either side of the 'O' ring appeared to be wet with fuel. Maybe this isn't made from Viton and the fuel has affected it

I don't know! So when fitting the stub flange to the Commando carb, I fitted a new 'O' ring, not from Amal, that I purchased as having been made from Viton. I also added an Amal paper gasket, with a light coating of Hylomar 300 RTV applied using a small artist's brush and bolted the stub and body together.
Mounted the carb and checked that the slide seats on the bottom of the venturi. Adjusted the air screw to 11/2 turns out from seated and the slide screw by 1/2 a turn in from starting to lift the slide.
Tomorrow, I will see if the engine starts any easier and whether I can achieve a steady tickover and clean pick up, with the 'SuperTrap' in place. If I can achieve this then I may try the Goldie again!
Good health, Bill