450 Desmo not running cleanly
Posted: Thu Feb 20, 2020 10:04 am
My 1974 450 desmo wont run cleanly after about 1/4 to 1/3 throttle opening. It seems to misfire and the more you open the throttle the worse it gets, until at full throttle it is totally bogged down and hardly running. Below that throttle opening it starts, idles and runs really well up to about 4500rpm which is usually where the problem starts. The bike was stored for about 20 years while life got in the way. About 2 years ago I started the process of getting it running again and for the last 6 months I have been riding it a couple of times a month sorting out issues as i go. Until now I haven't been revving it much while i worked through other issues, but now I need to sort this out......
As far as i'm aware the head and cams etc are stock.
The carb is a 29mm square slide with the following:
Main 135
Pilot 50
Slide 60
Needle New V7
Needle position 2
Needle jet New 262T
Float height 24mm. The float height was about 21mm - changing to 24 which I did today made no difference.
New carb gasket kit.
Inlet manifold gasket was not new but it was unused when I started to get the bike back on the road 2 years ago.
Fuel tank has been flushed and fuel taps are working ok. Fuel flow from taps to carb is fine in 1/4" fuel hose.
A week ago I installed a Sashce ignition to replace the original Electronica ignition. It made no difference.
Still using 6v electrics. Battery is putting out 6.3-6.5 volts.
I installed a new plug about 1500 kms ago. That didn't make any difference.
I'm leaning towards fuel being the issue, it just feels more like a fuel issue. But I am open to any suggestions!!!
Cheers
Dan
As far as i'm aware the head and cams etc are stock.
The carb is a 29mm square slide with the following:
Main 135
Pilot 50
Slide 60
Needle New V7
Needle position 2
Needle jet New 262T
Float height 24mm. The float height was about 21mm - changing to 24 which I did today made no difference.
New carb gasket kit.
Inlet manifold gasket was not new but it was unused when I started to get the bike back on the road 2 years ago.
Fuel tank has been flushed and fuel taps are working ok. Fuel flow from taps to carb is fine in 1/4" fuel hose.
A week ago I installed a Sashce ignition to replace the original Electronica ignition. It made no difference.
Still using 6v electrics. Battery is putting out 6.3-6.5 volts.
I installed a new plug about 1500 kms ago. That didn't make any difference.
I'm leaning towards fuel being the issue, it just feels more like a fuel issue. But I am open to any suggestions!!!
Cheers
Dan